Successful High Altitude Flight
For this launch, the altitude goal was 18.5km, or just over 60,000
feet. This altitude was achieved relatively close to the launch
site, and an hour or so after launch the glider released itself from the
balloon. It dropped into controlled and well-trimmed flight immediately
after release this time, correcting the expected few degrees of gyro
drift from the ascent with no problems whatsoever (field
photos).
Maximum G level during the pullout only reached 2.5g's, and maximum
true airspeed about 380 kph (205 kts). After pulling out into
level flight at about 57,000 feet, the glider was commanded to do a
panoramic photo turn (the circle on the chart below), and then return
home. Cruise airspeed was 230 kph (125 kts) or more.
It arrived back over the launch field with something like 45,000 feet
to spare, at which point we changed the glider from smart-pilot to
ground-commanded autopilot mode, and told it to take a few side trips
around the area to snap 35mm photos.
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The launch site is under the circles, lower right corner. We lost
a few minutes of telemetry when the windows printer driver crashed,
taking down the ground software. Note that the ground-commanded
photo excursion to the north and northwest occurred after the glider had
arrived overhead, and was at all times above 30,000 feet.
But the 35mm photos later turned out to be a great disappointment, as
none of the high altitude aerial shots turned out. Some
modifications made to the camera bay, sealing it up and using silicon
desiccant to reduce condensation, seemed to have badly backfired.
The condensation was so bad, most photos are badly
blurred. Next time, the opposite tack will be taken - gentle
venting of the camera bay with cold, dry outside air. Of course
this would all be simpler if "amphibious" landing-out hadn't
been part of the design spec, requiring it to be almost watertight.
The remainder of the flight from 30,000 feet down was spent in
smart-pilot mode, with the glider self-flying a tight approach pattern
over the launch field.
All systems worked perfectly, with the exception of the pressure
altimeter, which started to go a bit wonky above 55,000 feet.
Fail-safe routines finally tripped it out of service as the pressure
dropped below 9% of sea level, but the autopilot was able to use
GPS-based altitude to fill in the gap and estimate TAS, etc. The
pressure sensor came back into service as the glider flew below 55,000
feet again, however. This later turned out to be caused by temperature
drift of the baro sensor, which has since been adjusted for. The very
low ambient pressure at high altitude tends to strongly amplify the
effects of any baro sensor drift on the baro altimeter.
Winds were light from the west in the last few thousand feet, but
there was a moderate easterly breeze off the water within only a couple
of hundred feet of the ground, causing some inaccuracy in the
landing. Because the glider planning its final approach based on
the winds in its last circuit, several hundred feet up, it popped the
chute a little off from where it should have, and landed a few hundred
metres away from the set landing site. Not bad though, and it passed
within 11m of directly overhead as it flew upwind (or what it thought
was upwind) to pop the chute.
Although there were few decent 35mm photos this time, the quickcam
did work relatively well. Here are a few of the better shots which
were transmitted down during the flight:
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